After riding 85#1 more it wasn't popping out of gear, but it would miss shifts once in a while. Well I tore it down to investigate, plus it will be getting some hop ups. More on that later.
First off with its head!!!
Here it is headless
Ready to split the cases.
Cases split
Pretty much all apart
Now I did notice a couple things during the teardown that were broken or didn't look quite right. I think one of the broken pieces might be why it was missing shifts??? Any input will be appreciated.
1st I notice this spring not hooked right...
Then later found this in the cases....another part of the arm.
While taking the clutch apart the hub came out in pieces...
So hopefully Mr Kasey you can tell me if that arm was my problem. As for my plans for the hop ups:
88cc Big bore race head kit
stroker crank
cdi conversion
suspended frame kit
Probably a R55 kit since PK and A+ kits are so rare and hard to find.
With the mods it will be 110cc's and have more power than a chinese 125. I cannot take credit for coming up with the plans for this. I rode Steven0196's pk suspended 70 at TF with this same engine package. Had to have one so here goes my attempt.