Results 1 to 4 of 4

Thread: 1985 200X with a 1982 RM 250 engine. Long time ago, no pics

  1. #1
    Join Date
    Jun 2008
    Location
    NE Indiana
    --
    1,067

    1985 200X with a 1982 RM 250 engine. Long time ago, no pics

    I just wanted to say that I did this swap back when I was a teenager. I see a lot of people on here looking to upgrade their trikes and every time I read about it, that trike I built comes to mind. Here's the story;

    I had a 1985 200X and the engine blew. I had a friend who was unfortunately addicted to drugs (and I believe looking for drug money, thank God today he is clean and sober and has been for many years ) He had a beat up old 82 Suzuki RM250 with a good strong running engine. I told him I would give him 50 bucks for the engine to put on the 200X. Ironically he is the same person I bought the 200X from in the first place. He said yes, to the $50 offer and said "no way will you make that engine work". When someone tells me I can't do something that i think I can, I get motivated.

    To make a long story short, I was surprised at how little I had to do to make the swap work. I had to fabricate spacers for the rear engine mount but used the stock 200X bolt. I had my Dad fabricate the front engine mounts at his work. And he had a friend that he worked with that cut and re-welded the pipe to customize it to fit. I never got a silencer for it.

    This was back in the very late 80's early 90's when I did it but I believe I rigged the wiring from the 200X to run the RM engine but I can't exactly remember what I did for the wiring. But I'm 90% sure I used the 200X wiring/coil etc. to run the Suzuki.

    Anyway, there was little to it, to be honest. It was a bit time consuming to get the spacers correct to make the sprockets match up. But It was a 200X with an air cooled RM 250 engine and I will say, it was a very fun trike to ride.

    The spark plug was on top and I couldn't get to it without removing the gas tank. I found out the hard way that I installed the throttle slide into the carb backwards and the first time I ran it, it took off like a bat outta hell and the throttle was just wide open. No kill switch. No way to pull the plug wire. I tried upshifting to 5th to kill the engine but it just bogged for a second and took off again! LOL I eventually just pulled in the clutch and waited for my cousin to get there with a wrench to take off the tank and pull the plug wire. Wide open throttle, no silencer and just whaling away for about 2 minutes straight. I thought it was going to blow. But it didn't.

    I couldn't kickstart it because the kickstart was back kick and wouldn't work on the 200X. We had to push start it every time to start it. I was lucky that I had a good hill that led from my yard down to the trail and I just coasted down and popped the clutch and it started.

    I later sold it to a friend who later became my brother in law, and he rode it for a while and then sold it and where it is now is a mystery. I wish I could locate that trike today.

    Anybody from northern Indiana come across a 200X with a strange air cooled 2 stoke?


    P.S. For anybody who is wondering, yes, it did vibrate quite a bit.

  2. #2
    Join Date
    Oct 2002
    Location
    Northeast
    --
    17,460
    Hey bud, awesome post!!

    Glad to have "fabricators" on the board : !
    All our government does is distract us while they steal from us, misspend our tax $ and ruin our country

  3. #3
    Join Date
    Sep 2007
    Location
    British Columbia, Canada
    --
    818
    Sounds like an awesome build!
    Cool to know that there are other people who've swapped a 2 stroke in a 200X.
    Other than me, and one other person on .org, I hadn't heard of anyone else actually doing it.
    Mine's pretty quick so that thing must've ripped!
    Last edited by TwoHundredEx; 06-25-2008 at 10:51 PM.
    [b]'83 200X-
    White/Blue:
    The 2 stroke 200X
    Vids:http://youtube.com/watch?v=HwDqUVM9jOo

  4. #4
    Join Date
    Jun 2008
    Location
    NE Indiana
    --
    1,067
    Funny thing is, the RM 250 was basically the only engine available to me for the $$ at the time so that was the swap that was made. LOL.

    Yes, it was pretty fast and fun. I can't say it was wicked and out of control but it was very fast

//ArrowChat Integreation Code //