Hey Oscarmayer...........I know the #35 jet is opened up cause I did it with a drill bit when trying to unblock it. Waaaaaay too big. That's the reason for replacing that one. I'm trying a smaller one on the main because "I think" Honda, at the factory, purposely jets their trikes and bikes a little rich to protect themselves from lean damage. The Uni filter I put on should lean it out a little, too. I replaced the o-ring on the pilot screw. It was squished and a little tore at an edge. All the passageways are clear in the carb. Slide looks good. Needle looks good. I checked everything under magnification. The trike ran pretty good from 3/4 to full throttle, maybe 1/2 to full throttle. Ran like crap at 1/8 throttle just putting around in first gear. Idle was off and plugs were loading up bad just idling. Black as coal. They were black too even when doing WOT chops at full throttle in 5th gear, just one run up the alley with brand new plugs. I did three chops like that and that's why I figured I could go down a little on the main. I just want to see if I can optimize the performance for this stocky. I would have put a rebuild kit to it, but I don't personally think it needs one. If what I'm doing doesn't solve the problem, you can be sure that a rebuild kit is next on the agenda.



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