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Thread: 200x problems

  1. #1
    Join Date
    Feb 2013
    Location
    Walford, Iowa
    --
    120

    200x problems

    A couple weeks ago I was riding my three wheeler and it blew the head gasket out of it. I figured that since I didn't torque the head down properly that is what caused it to blow. But after I replaced the head gasket and put it back together it wouldn't even act like it was going to start. It would kick very easily and I wouldn't get anything out of it except for a small pop at the end. I was wondering if blowing the head gasket could cause the piston or the valve seals to go bad. Any help would be appreciated. Thanks

  2. #2
    Join Date
    Oct 2012
    Location
    Finlayson, Minnesota
    --
    1,066
    Depends.. how long did you run it with the head gasket blown? You could have heated up the machine.. having a head gasket leak makes it run lean as it is sucking in air.. hence why cars with blown headgaskets get hot from sitting. If you shut it off instantly then I doubt anything got wrecked. Only way to know for sure is if you do a compression test on it. I've blown a few headgaskets and nothing bad has come of it.. just replaced and ran it again.
    1986 250r - Fully rebuilt from the ground up!
    - http://www.3wheelerworld.com/showthr...ATC-250r-Build
    1985 Tri Z - Next project!
    1982 250r - Sold
    1983 Auto X - Sold
    1984 Auto X - Sold
    1985 200M - Sold
    1985 YTM 125 - Sold
    1985 185 - Sold
    1984 185 - Sold


    1/21/2013 - RIP Grandpa Rosa, great man, will be missed.. Love you

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  3. #3
    Join Date
    Feb 2013
    Location
    Walford, Iowa
    --
    120
    It started popping the day before so I'm betting it was sucking air. I didn't want to believe something was wrong since my and my buddies were riding them in a parade that day. So Im betting the piston is shot since it was sucking air for probably a couple hours of riding.

  4. #4
    Join Date
    Apr 2010
    Location
    Indian Falls, NY
    --
    1,289
    Luckily these engines are simple to work on....I just hope you haven't done a lot of work to it. That would be just wasted time.

  5. #5
    Join Date
    Sep 2011
    Location
    New Castle, PA
    --
    1,134
    If it ran like that for a few hours, i say that you probably scored your piston and cylinder wall and destroyed your rings, but no way to know until you get into it. if the piston and wall check out (no damage, within tolerances), then get a new head gasket, buy some rings, and have at it.
    1983 212x "Mickey Dunlap" Powroll TT Trike -Blue frame, Supertrapp (looking for a Powroll DD), WEB Stage II cam, Powroll 6mm stroker, Wiseco 10.25:1 piston stock bore, ported, polished, +2 Swinger,White low-pros and 250R front fender, BAPP rear shock, Powroll Decals, NOS Carlisle R/A's

    Gone:
    '83 185s, '86 200x, '70's Full Suspension Hi-Performance ATC RD400,

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